Before we attacked the problem, I did some research on the Web and learned that the design of the fresh air intake on the Mustang was poor to begin with, and Ford didn't help matters by assembling the cowl as a two-piece unit with no paint on the inside. This automatically ensured that rust would begin forming after the first rain or washing that the car endured. In addition, if the car was left outside, leaves and other debris would pile up inside the cowl and eventually block the drain holes. Once this happened, it was only a matter of time before the forces of nature would eat their way through the sheetmetal. Once that happened, the floorpans were doomed to the same fate. After reading all of this, I felt more than a little frustrated at Ford (and all American manufacturers, I'm sure) for basically ensuring obsolescence in their product. Is it any wonder that many Americans used to buy a new car every two or three years?
So, putting aside my frustrations, I picked up a grinder and
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| Opening up the drivers side of the cowl |
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| Rust holes around the outside of the "hat" |
Since we're still trying to maintain somewhat of a budget, and the project is dragging somewhat, I decided to try and fix the holes without removing the top half of the cowl. This is a very labor-intensive process that requires the removal of around 200 spot welds. I knew that if we started down that path, Daniel would become completely demoralized!
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| Note the big hole in the lower right |
gave each side a liberal coating of Rust Seal, the super hard epoxy paint that we're using on the underside and floorpans. My thinking was that if I sealed the metal from future corrosion, I could also create a good bonding surface for fiberglass matting in there and form it around the hats, effectively fiberglassing them in place.
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| Applying fiberglass |
both bond to the old metal and seal out any future water contact to the old rusted areas.
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| Plenty of seal sealer should do the trick |
Undeterred, I took stock of the situation. I quickly identified (what I thought was) all of the remaining pin holes and gaps. More caulk was applied. More water was poured in. More water flooded into the car! More resolve was made to stop the leaks!
We did this routine a total of five times.
I could tell Daniel was getting a little tired of the process, but I tried to impress upon him the importance of this repair, probably
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| The first bucket test...or the second? |
After the first and second tests, I spent more time under the dash trying to figure out exactly where the leaks were that evaded my repairs. I finally determined that the front seam of the cowl assembly, which is only spot welded, was letting water through to the interior. We both agreed that the only reason that water was getting through there was due to the volume of water that we were pouring in at one time, which was probably more than anything that would occur in normal use. However, since I had figured out the hidden problems, it made sense to keep caulking.
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| Closing the patient back up! |
For final insurance, I applied another liberal coat of Rust Seal over the seam sealer, to fill in any possible pin holes or little spots where water would accumulate.
Finally satisfied with our efforts, it was time to weld up our holes.I feel pretty pleased with the end result. Now we can move on to the final bit of sandblasting in the engine bay, and start some reassembly!






